
The servo motor was fairly easy to wire. I added headers to connect it to the board. Starting with the code from the website in class, I added a blinky and programmed the chip.
At first the motor did not work. I checked the connections and tried again. This time, it vibrated. I think it may have been that the connection between the motor and the board was not good so I covered it with electrical tape and tried again. Success!!
Next step, getting the servo motor to work with the pot.


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